Damage Caused by Low Speed Engine Firing Impulse and the Repairs
With Victor 1+ engine flight time approaching 47 hours, and having gotten rid of the yaw trim problem and lowering the thrust line, the FireFly was slipping nicely through the air. I felt it was time to go the final step and to limit engine power output to 38 hp (5,200 rpm on the Victor 1+) by increasing propeller pitch so the FireFly would meet all AC 103-7 requirements.
I increased IVO propeller pitch and flew the pattern to determine maximum engine rpm, and then on the ground added more pitch and repeated the process. When the engine was limited to 5,400 rpm, I realized that I was in trouble. The FireFly flew well, but on the ground it was another matter. Even with the engine idling at 1,000 rpm, one had to excessively ride the brakes while taxiing. The inertia of the 56 inch propeller was low but the engine firing impulse was shaking the cage. I decreased propeller pitch and flew again and found the engine topped out at 5,800 rpm. On this pattern circuit, engine noise increased.
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Some of the tabs that located the coolant recovery bottle bottom were broken or missing. I had used a hose clamp to hold the top, but when the bottle has coolant in it, most of the mass is at the bottom of the bottle. When things get to shaking, it is the bottom of the bottle that must be restrained. A new base was made out of stainless steel and lined with red electricians tape to prevent scuffing between the bottle and the stainless steel.
The above is a good example of how a change in engine loading after 40+ hours of operation had a destructive effect on components that previously had shown no signs of stress or failure. The sad part of all of this is that the Victor 1+ engine will have to be replaced if one wants to keep the FireFly an ultra light vehicle.
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